![]() Seems to be a rather large bug in the newest firmware. – All channels are functioning fine, with the Naze32 receiving the yaw input from the receiver. – Servo signal wire is connected to pin 1 of the Naze32 (S1 in servo mode) – Servo works with both a servo tester and when connected to one of the ESC pins on the Naze32 I tried to flash the Naze with Triflight but after doing some researched I realized that I have a Naze32 REV6 when the firmware was designed for a REV5. – Servo is powered by a separate voltage regulator (5V) I was using a Multi wii FC but just switched over to a Naze32. – Servo is a Turnigy TGY-211DMH (coreless digital) I suspect this is because of the new IMU on Rev6 which isn’t supported by the old firmware. I’ve found that flashing to 2015.07.11 makes the tail servo respond to inputs just fine, but only acro mode is available (see screenshot). I just installed a new Naze32 rev6 onto my RCExplorer frame, and I can get no response from the tail servo (either via rudder input on transmitter, or as a counter-reaction to yaw) using firmware 2015.08.27. I hope this is where the tri guys hang out!
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